TTEC4842 - Automotive Engines - practical
18/10/2011 tuesday
start = 1.00pm finsh = 4.30pm
Engine Short Block
(Enigne short block)
first thing i started with the engine block was taking everything apart from the block pistons, conrods, crankshaft, ETC
Inspection of pistons
first thing i started with was Inspection of the piston, which i had no pistoon damage on all pistons , no scarfing, so the pistons were in good condition.
Then moved on by measuring the piston diameter, by using a micrometer.
1 | 2 | 3 | 4 | |
piston | 77.93mm | 77.96mm | 77.97mm | 77.97mm |
ok/fail | ok | ok | ok | ok |
This showed me that the piston were all ok and dont need replacing.
Inspection of cylinder bore
First thing was to inspect the `bore of the block and there was no sign of damage or any scuffing.
then moved on by measuring the bores with a bore gauge at two positions top, , bottem.
Cylinder bore measurement.
cylineder 1 | cylinder2 | cylinder 3 | cylinder 4 | ||
1 | first measurement ( direction x) | 78.05 mm | 78.051mm | 78.051mm | 78.051mm |
first measurement ( direction y) | 78.05mm | 78.051mm | 78.051mm | 78.051mm | |
3 | third measurement (x) | 78.05mm | 78.05mm | 78.05mm | 78.05mm |
third measurement (y) | 78.05mm | 78.051mm | 78.05mm | 78.05mm | |
amount of taper | 0.0mm | 0.0mm | 0.00mm | 0.00mm | |
amount of ovality | 0.0mm | 0.001mm | 0.0mm | 0.0mm | |
ok/fail | ok | ok | ok | ok | |
this showed me that the cylinder bore measrement meet the specifications some which were 0.1 mm of but didnt matter
Piston clearance
cylinder 1 | cylinder 2 | cylinder 3 | cylinder 4 | |||
(a) | largest boren diameter | 78.05mm | 78.051mm | 78.051mm | 78.051mm | |
(b) | pistoon skirt diameter | 77.93mm | 77.96mm | 77.97mm | 77.97mm | |
piston to cylinder clearance(a-b) | 0.12mm | 0.091mm | 0.081mm | 0.081mm | ||
ok/fail | ok | ok | ok | ok | ||
this showed me that all four pistons were in the manufactring specifications.
piston and rings
first thing was i did a visual check on the piston rings for any sign of damage, wear or breakage,.
four of the rings were in good condition, so they dont need replacing.
then moved on by checking the clearance of the piston rings using a feeler gauge between the ring and the ring groove.
ring side clearance | |
specification 0.030mm-0.065mm | |
1 | 0.051mm ok |
2 | 0.051mm ok |
3 | 0.051mm ok |
4 | 0.051mm ok |
this showed us that the rings clearance is good and it meet the specification. if the rings have any excessive side clearance. if by if the lands wear our or the rings wear out aswell.
checking piston ring end gap
first thing was i put the ring into the cylinder bore, then push the ring down the bore, using the piston to keep it square, until the ring is in the least worn part of the bore. then i checked the ring end gap with a feeler gauge.
top ring end clearance | |
specification 0.15mm - 0.30mm | |
cylinder 1 | .229mm ok |
cylinder 2 | .229mm ok |
cylinder 3 | .229mm ok |
cylinder 4 | .229mm ok |
Inspecting connecting rods
first thing was is to inspect the rods for any bend twist or any misaligment. i checked my rods is by using the tool called hydrulic rod straightening press.
bend | twist | ||
1 | 2.95mm | .508mm | |
2 | 1.09mm | .254mm | |
3 | .813mm | .505mm | |
in this task we couldnt use our rods we used different rods and couldnt get the manufacturing specifications.
Inspecting the crankshaft
main journal specification
main journal specification
diameter = 0.05mm
taper limit = 0.05mm
ovality= 0.05mm
In this task was to measure the main journal using a micrometer to check for (A) which is across and (B) down.
1 | 2 | 3 | 4 | 5 | ||
diamater A1 | 49.49mm | 49.46mm | 49.45mm | 49.45mm | 49.45mm | |
diameter B1 | 49.96mm | 49.45mm | 49.44mm | 49.40mm | 49.45mm | |
diameter A2 | 49.94mm | 49.43mm | 49.46mm | 49.46mm | 49.45mm | |
diameter B2 | 49.93mm | 49.45mm | 49.45mm | 49.45mm | 49.46mm | |
ovality A minus B | 0.04mm | 0.01mm | 0.01mm | 0.05mm | 0.00mm | |
largest diameter A1 or B1 | A1 | A1 | A1 | A1 | A1,B1 | |
smallest diameter A2 or B2 | B2 | A2 | B2 | B2 | A2 | |
taper A1 minus A2 | 0.00mm | 0.03mm | 0.01mm | 0.01mm | 0.001mm | |
STD diameter | 49.956mm | 49.956mm | 49.956mm | 49.956mm | 49.956mm | |
smallest diameter (from A or B ) | 49.94mm | 49.43mm | 49.45mm | 49.45mm | 49.45mm | |
wear | 0.506mm | 0.506mm | 0.506mm | 0.506mm | ||
Big end journals
big end journal specification
diameter = 39.94mm
taper limit = 39.94mm
ovality= 39.94mm
inspecting the cylinder block
1 | 2 | 3 | 4 | |||
diameter A1 | 40.70mm | 40.70mm | 40.70mm | 47.70mm | ||
diameter B1 | 40.94mm | 4.94mm | 40.93mm | 40.94mm | ||
diameter A2 | 40.93mm | 40.94mm | 40.94mm | 40.93mm | ||
diameter B2 | 40.94mm | 40.94mm | 40.94mm | 40.93mm | ||
ovality A minus B | 0.24mm | 0.24mm | 0.23mm | 0.24mm | ||
largest diameter A1 or B1 | B1 | B1 | B1 | B1 | ||
smallest diameter A2 or B2 | A2 | A2 | B1 | B1 | ||
taper A1 minus A2 | 0.24mm | 0.24mm | 0.23mm | 0.24mm | ||
STD diameter | 39.94mm | 39.94mm | 39.94mm | 39.94mm | ||
smallest diameter (from A or B ) | 40.93mm | 40.94mm | 40.93mm | 40.94mm | ||
wear | 0.99mm | 1mm | 0.99mm | 1mm | ||
This was a havey duty crank shaft , and the undersize 0.50mm this was in good condition and meet the specifications.
inspecting the crankshaft
crankshaft deflection specification. Runout 0.04mm ( 0.0016 in ) mm
first thing i put the crankshaft on the 'v' block to measure the crankshaft deflection. which i measured by using a dial test indicator (DTI)
The run out was 0.00mm there was no distortion.
inspecting the cylinder block
did a visual check on the block there was minear scuffing on the top.
The moved on by measuring the cylinder block face distortion in six places.
block face distortion specification .05mm
The moved on by measuring the cylinder block face distortion in six places.
block face distortion specification .05mm
6 of the test on the block face distortion were 0.00mm they were in the distortion specification.
Inspection of timing gears, sprockets,chains,and belts.
camshaft gears or sprockets= there was no damage or wear on the camshaft
crank gear or sprockets= it was clean no wear or any sign of damage
idler gears or sprockets= the tensioners are nice and clean no sign of damage
this showed a good resultsn there was no damage or any wear on the timing belt.
inspect water pump
there was no sign or damage on the water pump, just needed new idle bearing replaced.
inspecting oil pump
the type of oil pump i was working on was a rotory pump. i did a visual check, the rotor pump looks in good condition no damage or any signs of scuffing.
checking clearance
specification | actual | |
gear or lobe to housing | 0.05mm | .004mm |
gear backlash | 0.05mm | .004mm |
gear lobe to end plate | 0.05mm | .004mm |
gear to crescent | 0.05mm | |
The oil pump is in good condition and its serviceable.
checking main bearing oil clearance
first thing i did was placed a strip of plasti-gauge across each main journal
Main bearing clearanceThen i installed the bearing and caps to torque specification 54-59 mm
Then i removed the caps and bearing and measured the widest part of the plasti-gauge
The oil clearance were in the specifications.
Main bearing clearanceThen i installed the bearing and caps to torque specification 54-59 mm
Then i removed the caps and bearing and measured the widest part of the plasti-gauge
specification 0.024-0.042mm | |||||
1 | 2 | 3 | 4 | 5 | |
oil clearance (actual) | 0.038mm | 0.038mm | 0.038mm | 0.038mm | 0.038mm |
ok/fail | ok | ok | ok | ok | ok |
The oil clearance were in the specifications.
checking crankshaft end play, using The (DTI) first things i set the gauege to Zero and i pulled the crankshaft towards the DTI and i had reading of zero there was no end play on the crankshaft
checking crankshaft end play using the feeler gauge
specifications'0.08-0.242
End play 0.09
specifications'0.08-0.242
End play 0.09
This showed that the crankshaft is in good condition and meet the specification
checking the big end bearing clearance
checking the big end bearing clearance
i used the same meathod for the main bearing by using a plasti-gauge across the connecting rod journal.
specification 0.024-0.042mm | |||||
1 | 2 | 3 | 4 | ||
oil clearance (actual) | 0.038mm | 0.038mm | 0.50mm | 0.038mm | |
ok/fail | ok | ok | ok | ok | |
the big end bearing clearance also meet within the specification. i ensured that the crankshaft also should turn freely before doing the measurments.
checking the connection rod end play, using a feeler gauge.
specification -0.30mm | |||||
1 | 2 | 3 | 4 | ||
con-rod-endplay (actual) | .559mm | .457mm | .457mm | .599mm | |
ok/fail | fail | fail | fail | fail | |
this showed me that my cond rods fail within the specifications because there was a big end play. this means they need to be replaced with a bigger once.
IN conclusion
the block i was working on was a haveay duty block which i worked on. the block was nice and clean looked in good condition. there was no damage on the pistons or the rings. the rods were nice and strait. there was couple of bolts missing on the block before i started working on it. but the block i worked on was nice and in very good condition.

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